Originally Posted by
performance
There are a couple of "other" possible issues, both related.
1) The wrong side of the drive roll is being used. It seems to me that the way my unit came is with the .040 side set to use. It looked like the .035 would work, but it just wouldn't. I flipped it over to the .030 side and haven't had any more issues. The drives are for .030/.035 and .040/.045. I also had to experiment with drive feed tension. I found out about 3/4 of the way down is best for my unit. You may find different requirements for different type spools and the resistance they provide to "turning". I keep mine more loose than tight. Make sure the wire is down in the groove. I have changed it out in the shop where light wasn't as good and found the wire wasn't in the groove, but it was still feeding...but not real good.This will have a lot to do with the way the unit welds.